For the nicker, I had to do some head scratching. Vintage models use a
wedge to hold nickers in place, but I didn't feel like fitting a wedge.
And, the alignment issue was also on my mind. What I finally decided on
was a pair of hex-key set screws. One comes through from the other side
of the body of the plane, just at the bit of the nicker. The other is
about 3/32" above it, tapped into the metal plate on the side of the
plane. The lower screw allows me to align the bit with the side of the
plane. The screw through the plate clamps the nicker in place.
The
blade required some fine tuning at the wet grinder to get the angle
just right, but it sharpened up just fine. After that, I put everything
together and made a few test passes.
When
I resoled the plane originally, I made a very tight mouth and throat.
But because the shavings are cross-grain, they break off pretty easily,
and not only is the support of a tight mouth not really needed, but it
jams up pretty quickly. So, I opened it up. Because the blade is
basically plowing out material, and not leaving a final surface, I'm ok
with this. (I'm more worried with keeping the shavings flowing, than how
finely they're being cut... this is intended to be a production too,
despite the fussiness I've been putting into it.)
After
that... well, that's pretty much it. I made a few more test passes with
the plane, and it worked like I'd hoped. So, I gave it a good coat of
wax, and played around with it for a while. Next week I'll get to put
this tool to work.
Read Part One.
Read Part Two.
Read Part Three.
Read Part Four.
The Plane In Use.
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